JxxxOxxxE
11-09-2011, 10:22 PM
I'll try to make this short....
..basically bought a basket case 250r with some good parts here and there....Had a CT 330 cylinder with it with a messed up sleeve...Had it re-sleeved locally, sent back to CT to have port matched for a stroker. New +4 crank, new bearings, new 76mm piston and had bored locally....
PWK 39 mm carb with 52 pilot and 190 main, ESR trx MX pipe...compression checked before initial start up was ~160 (seemed low to me), started on 110 gas with 32:1 mix
Started it up for the first time yesterday, drove it around 3 or 4 times, never going over 1/2 throttle, short 5 minute runs. Started it up today rode it another 2 or 3 times for short runs today...
Then decided to take it out and go 3/4 throttle or so....After about 10 minutes of riding, it locked up under about 3/4 throttle...Get it back home pull the plug, its unlocked now, comp test shows 150....decided to tear it down anyway...Here's what I've got...
http://img213.imageshack.us/img213/4941/img2335j.jpg
http://img402.imageshack.us/img402/5644/img2336n.jpg
http://img832.imageshack.us/img832/9049/img2337xw.jpg
http://img804.imageshack.us/img804/6025/img2340b.jpg
http://img810.imageshack.us/img810/15/img2344c.jpg
http://img208.imageshack.us/img208/8836/img2345e.jpg
So....doesn't look like it went lean to me, the plug doesn't look lean to me....
Was this bored to tight? That's really my only thought right now....
The ride it locked up on, 10 minutes, was the longest ride since it was put back together...
Any ideas or comments are appreciated...
..basically bought a basket case 250r with some good parts here and there....Had a CT 330 cylinder with it with a messed up sleeve...Had it re-sleeved locally, sent back to CT to have port matched for a stroker. New +4 crank, new bearings, new 76mm piston and had bored locally....
PWK 39 mm carb with 52 pilot and 190 main, ESR trx MX pipe...compression checked before initial start up was ~160 (seemed low to me), started on 110 gas with 32:1 mix
Started it up for the first time yesterday, drove it around 3 or 4 times, never going over 1/2 throttle, short 5 minute runs. Started it up today rode it another 2 or 3 times for short runs today...
Then decided to take it out and go 3/4 throttle or so....After about 10 minutes of riding, it locked up under about 3/4 throttle...Get it back home pull the plug, its unlocked now, comp test shows 150....decided to tear it down anyway...Here's what I've got...
http://img213.imageshack.us/img213/4941/img2335j.jpg
http://img402.imageshack.us/img402/5644/img2336n.jpg
http://img832.imageshack.us/img832/9049/img2337xw.jpg
http://img804.imageshack.us/img804/6025/img2340b.jpg
http://img810.imageshack.us/img810/15/img2344c.jpg
http://img208.imageshack.us/img208/8836/img2345e.jpg
So....doesn't look like it went lean to me, the plug doesn't look lean to me....
Was this bored to tight? That's really my only thought right now....
The ride it locked up on, 10 minutes, was the longest ride since it was put back together...
Any ideas or comments are appreciated...